The customers complaint was the Ac was not cooling, and I found the breaker was tripped but the problem took a bit to find...
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I'm gon na use an impact, but it's okay, because i got that trigger control. This video is brought to you by sportlin quality integrity and tradition um. This is the restaurant, where i had a restricted expansion valve and we ended up having to change the dryer too. Actually, we had a restricted dryer and the expansion valve was gummed up.
Um customer called and said the kitchen's still hot. So i came here and the kitchen's 75 degrees. The ac is working, it's kicking butt, but as i you know, they were saying like. Oh man, you know it's still not working, and so i'm driving back out here, i'm thinking, okay, the compressor failed or whatever no everything's running uh.
It doesn't. I mean i haven't, put gauges on anything, but it's not restricted. Suction lines are cold, uh every you know, vital signs seem fine and it's nice and cool in the kitchen. But in talking to the customer they said yeah - and you know the dining room's hot and i said, wait dining room something totally different.
This is the kitchen. So they said yeah the dining room's hot too. It's like okay! Well, as i was walking up on the roof. I noticed that this is their dining ac right here, and i noticed that the main breaker downstairs is tripped for this ac.
So we need to open this guy up uh power it down up here and reset it and figure out why the main breaker would have tripped downstairs now why they're complaining about the kitchen ac, i don't know you know i'll, look and see. So what i did was i powered down at the disconnect switch right there and then we're gon na go downstairs, reset the breaker and then come up here and test everything come over here. Rtu 2 is tripped. It's in the mid position so turn it on.
It. Doesn't do anything off then on um, don't see any issues there we're going to check voltage we're going to do visuals before we turn everything on open everything out to ground nothing's. Jumping out at me electrically. We look.
Okay, don't see any major shorts that i know of at the moment it's pretty big if it tripped a main breaker and didn't blow like a fuse or something so all right, uh the power's off to the unit belt's snug, no funky noises don't see any burnt. Anything wires, nothing scary see how the filters are filters, look relatively clean, these are from the filter. Changer, don't see any issues there, huh, okay, i tested three phase at the disconnect switch. It was correct, 2083 phase, so we're going to go over here.
Grab our meter and start checking at these compressors. This is an 18 ton, so we got four compressors in it. We're going to tone everything out, make sure we don't have any direct shorts i'll, show you what i find so i've tested every compressor to ground. I get nothing.
I've tested the resistance across the pins on each compressor and they're all fine. I get no direct shorts to ground on the load sides of the contactors. I also don't get any direct shorts to ground on the line side of the incoming power. I pulled the wires off of these capacitors and tested the capacitors while they were sitting here, and i do have some capacitors that are bad. Three of them are actually measuring really low i'll show you right now: uh 10 microfarad capacitor, the first one is measuring 10.21. Let's jump on to the next ones, so on these capacitors it's uh, let's see plus or minus six percent on this one. So it's running 10.21 we're allowed to run 10.6 so that one's good, this one's plus or minus 10 and it's running 7.5 so that one's low for sure 2.8 on the third one, so that's definitely low and 8.1 on the third or fourth one. So all three of these are low for sure, but i don't quite know if that would cause me to trip a breaker.
I would expect that i would blow a fuse. No, those are 30 amp fuses. I mean we tripped 150 amp breaker, we're looking for something grander than just a bad run. Capacitor for a condenser fan motor for sure, we're looking for a big boy problem hold the cover off of the contactors.
They certainly don't look great, definitely kind of caked in there. Let's move on down the line, yeah those look horrible, i've seen worse, but oh yeah. Those things are toast. Now that would definitely cause us to run high amps.
I still don't know about tripping 150 amp breaker, but maybe, depending on how low it's going, how hot the compressor is getting. Okay, we're gon na keep on going, i'm just going to the common places on these guys and these blower motor wiring. I've seen these rub out before no nothing so there's definitely been rubbing on the bottom of the unit right there, but i don't see it's not messed with the jacket at all. So the jackets don't look messed up, huh.
Well, i've done about everything i can to make sure there's no direct shorts and i'm not seeing any. So at this point um, you know one last thing: i need to check those fuses right there, but at this point i'm ready to turn this on. So i'm gon na check those fuses real, quick, okay, fuses are good um. Let's fire, this guy up hope nothing blows up.
Sometimes you just got ta. Do everything you can to try to isolate, find things can't find it flip it on and see what happens? This? Guy should fire up into full cooling here test current draw see where it's running at indoor blower just kicked on it's taking too long, i'm gon na put it in the test mode. Do it real, quick we're waiting for the stupid, thermostat interesting, we're running 1.3 amps of current from just the board alone and the transformers all right, so we're going to go c11! That's going to kick! That's going to give us a heavy start, because that's going to kick everything at once, i'm going to step back when this pops on we go all four running 76 amps 78 amps he's cranking 80 compressors running really hard uh all, but one condenser fan motor running Is that, oh that's this i was like: why is it vibrating? It's a stupid thing, so condenser fan motor, definitely not working 78 amps, and this is a heavy heavy call. This thing's running we're going to do some voltage drops across the contactors, see what those are looking like. So the fla on the blower is uh 15.7 and we're running. Actually, i think it was higher than that. What was it? Let's go over here, verify evaporator motor 16.7 and then the compressors are all 14.7 so 16.7 on the blower, which we were fine right at 15.. Let's test the compressors 11, so that's cool 10.7, 11.
12. 13., that's kind of high! That might be the one where the condenser family 14.3. Okay, so we need to get those condenser fan motors up and running. Oh that other one started finally, but we're running high current on the compressor, but it's it's running backwards.
Actually so we're going to change those capacitors and see if we drop that current down and see if those compressors calm down, when we do that too, i just cleaned this condenser. So it's not a dirty condenser. So these two are amping on the high end, but they might be part of those condenser fan motors that aren't working right, so we're gon na go see. If i got three caps in the van okay caps are changed out.
Let's fire this guy back up again. So we're gon na go to c11 full unit test, wait till the decimal appears and back away all running 76 amps, and i i was incorrect. It's a 100 amp main breaker. All condenser fan motors should be running right now this one's running.
Now too, we're going to test them test current on them find out. I think it's 2.4 is what they can run. So these are my motors right here. The relays don't look good either the little ice cube relays and i can see that some of them are burnt, so we're allowed to run 2.4 so 2.1.
1.66. 1.7. 1.8. So that one that's running 2.1, oh yeah, 2.22.
That says condenser fan motor number. Three. That's the one that had a bad cap and it's running really. It almost seems like it's running slow, so we're gon na change that condenser fan motor, my goodness gracious the heat coming out of that condenser right now.
Uh is insane and i'm about to get a a rain cloud right now. If you look over here, we got thunderstorms coming as i was coming out here. It was raining on me, so that's my temp in the shade 107.. Let's see what it is out in the sun, so it's about 114 in the sun.
It's like about 133 discharge, air temp, it's hot man, this thing's moving air. Like i said i recently cleaned it. I didn't i mean i took the side panels off and stuff. So it's it's moving air, but you know what man listen.
Can you guys hear that it sounds like a dry bearing i'm getting like a dry bearing sound from this guy there it is there. It is, i think, that's the indoor motor, i think. That's the indoor blower motor there it failing it's so hard to tell if it's the motor or that back bearing it's. Definitely the motor okay makes me feel a lot more comfortable. You can hear it in there without the belt. I was trying to figure out because the sound was resonating in the back, but definitely definitely the motor. This is what i'm talking about. When i say you got to use your senses, ditch the headphones when you're on the roof.
Okay, headphones have no place on a roof unless you're in, like a mechanical room where you have to use them for hearing protection but up on the roof. I'm just working on this unit and i'm listening, and i can hear this weird sound. You know - and i didn't hear when i started it up, but i'm starting to hear it just a little bit at a time and and it's this you know now - this belt is too tight for my comfort, as it is pulley's. Interestingly, worn this one's really uh sharp on the edges too, it's kind of weird.
I don't think it's a aligned properly, the belt's kind of worn right here and it's really sharp, but um yeah that guy's a little bit too tight. So we're going to loosen this up too just to get us a little more life out of this yeah motor's, really hot. So we've got a dry bearing in that motor. So i can see you guys, aren't gon na be able to see in here, but i pulled these grease ports off and there's grease in there, but there's not very much.
It's rather dry. I can see the shaft rotating, so we're gon na put a little grease in there. I'm still going to talk to them about replacing this motor, but we're going to see if we can help them out a little bit. These things don't have a port for grease.
It just has these little fittings right here that we're plugging it off, but what i did was i took the zerk fitting out of the pillow block, bearing temporarily put it on this guy, just greased it until it started coming out the shaft just a little bit Again this is this: is just gon na get them by um, probably not using the right grease either. I don't even people always ask me what grease i use. I just whatever the supply house has. I really don't pay too close attention to that um.
So we're gon na grease this one up too, but i wish i could show you guys the inside of that thing, but it's completely dry. You can just see remnants of grease since i got the grease gun, i'm to go ahead and grease this bearing right here and that bearing right there. The sheet has two bearings. Also, when you're applying grease to these bearings into the motors, you should be spinning it as you're applying grease and you don't want to over apply you don't want to.
You know just jam the thing full of grease. I just basically lightly filled it up and that's it just slightly when it started pumping out the seal right there, not even the seal, but the shaft um just lightly, though so, and then we're gon na. Do this one and i'm gon na loosen this belt up and don't be that guy always clean off the grease when you're done make sure you get it all off that way, there's not a massive amount of grease and then run inside the race of the bearing Get the old grease out of there try to clean up after yourself as best as possible. Okay, this guy's ready to go back in now, it's a little looser than i'm comfortable with, but it's better than it was everything's greased up we're gon na fire. This guy up see, if it calms down with that sound it was making still making it give it a second. I could hear it from the outside of the unit. That's a problem. I've got it in test mode right now, when the unit goes into test mode.
It powers down the unit, but the indoor blower contactor still pulled in, even when i take it out of test mode. You should usually hear the unit completely stop and there's a number 50 error codes, because i messed up the limit switch when i was pulling the blower assembly out so that should have shut off by now, and it's not so there's something wrong with the m2 or M17 board - i should say i don't know if this unit's going to be worth fixing with this customer they're, probably going to want to replace it, because if they're going to need a board, contactors condenser fan motor indoor blower motor pulleys i'll bet you anything. These guys will replace it and the crappy thing is: they need to replace this unit, this kitchen, the one that had that compressor issue before they changed that all right we're gon na. Let it run for a bit, see how it does you know what i'm wondering.
That's something to do with that limit switch in my head, i'm trying to think if they will, if you have a bad limit switch if they'll run the indoor blower motor as like a safety precaution, i need to investigate that before. I condemn that board yep! That's what i thought it was uh. I just jumped out the limit switch temporarily and now the blower shuts off. So it's it's a function like a safety function in case the limit switch ever failed and heating.
It just automatically runs the blower, even if it's in test mode. So what i'm going to do is lock out the heating, because we're not going to use the heating anytime soon and then we'll order that lemon switch when we come back so the m2 is not a problem, are they prodded or that i'm sorry m1a board? So all right, i'm about done man, i'm beat i've been drinking water like a fish, i'm just dying, it's hot um and it's humid out here for us, it's probably like 30 or 40 humidity, california. That just kills us. We don't know what humidity is here.
So i'm wearing a long sleeve, an undershirt sweating like a pig um all right, so that's all i can do for now. I just bypassed the limit switch, we'll uh, i locked out the heating so that we won't turn on we're going to talk to the customer. See what they want to do so indoor blower motor pulleys condenser fan motor contactors um. I should put my gauges on it, but i'm not really in the mood right now and uh. This storm is about to be here, so i need to get out of here. It's raining already over here. I can see it so as far as this unit, i don't know what to tell them. They said it was 86 in the kitchen.
Yesterday, 75 in the kitchen, when i got here today and this thing's cranking no problems at all. No restrictions, i mean everything's cool with this guy, so i don't know i'll tell him to keep an eye on that all right. We're back. Today, we've got a new indoor, blower motor motor knitcha fan motor blade, pulleys belt.
All that fancy stuff uh. Let's take a look at this kitchen, ac that i was here on the one that had a plugged up filter dryer. We don't have any active codes, nothing new customer hasn't complained. So hopefully all is good.
At this point. We're gon na go ahead and get started on that dining room. Ac, though the unit's running full call for cool and uh. It looks like the uh.
The motor held up didn't trip the breaker anymore. It's been a couple weeks since i was last here so greasing that thing up temporarily helped to get them through we're still going to go ahead and replace it, though pulled it out for easier access, and then i went ahead and put some uh penetrating oil on Everything all in here while i start sanding everything up. I also verified that the parts i have a pulley pulley and a bushing right there, they're all the correct parts, so we're good on that. So we're just gon na get started on this.
I also powered down the unit and made sure we didn't have any power so we're good to go. Okay got some sandpaper here, start by sanding everything up once we get it. Sanded up, start disassembling, loosening, bushings and all that stuff work. The sandpaper right.
You get! These real thin strips you can actually turn the shaft with the sandpaper makes it nice same thing for this, so i'm cleaning up the inside, so i could potentially, if i have to push the pulley onto it. In fact, you know what i don't need to take. This one off, because uh i've got a whole new motor, so we're just going to get this one off all right, so the bushing right here i pulled the screw or the the bolts that hold it together that sandwich it together and put them in the opposite. Holes so now we're going to push it apart and you're going to put even pressure on both sides, and then it also looks like we might have a set screw in here that i need to pull out so we'll check that set screw real, quick and then We'll uh start separating the pulleys yeah we're gon na apply even pressure, so one quarter turn one quarter turn just keep going all the way around.
Don't do it evenly, though it'll pop off spot free right off, so this motor hasn't been maintained and hasn't been greased for a very long time, and that's mainly why i'm changing it, because the bearings have basically overheated and potentially have damage. Now it's not making the whining noise anymore, but it's been so long since it's been greased that it. You know it's just time to replace some of these things. This customer's so far out here that it's not worth it for me to try to grease it and come back and because the callbacks and the amount of labor that i would have to charge them is ridiculous, so transformations got it yeah. We need to set this guy where the other one was set, so we find the old motor and i'm going to set it based on the old motor settings, which is all the way closed, we're going to start there. So on this one, you got ta pull this set screw then pull that key out and then you'll be able to adjust it and tighten it all the way. Okay. Now we want to go ahead and put a belt on, so we can get a ballpark and it'll help us to do the alignment.
Let's see how tight this is. Okay, that's too tight! So we're gon na go ahead and loosen it and then tighten it up. I'm gon na use an impact, but it's okay, because i got that trigger control. Okay still loose.
Now we can kind of set our depth yeah, i'm just using an eyeball to get me in the ballpark, keeping in mind that when we tighten this uh taper down or this uh bushing going to pull the whole pulley that way, so we want to set our Level ever so slightly in because when we tighten it, it's actually going to pull the pulley onto it. So that's pretty close. Now everything is finger tight when it comes to the set screws and everything we don't use an impact for any of this, because we'll end up breaking everything. Okay, now we're going to tighten evenly that's about it.
We make sure that we look straight looks good, looks like we can go in just a little bit that looks dead perfect. I, like it a lot okay, that guy's already torn down and then now we just need to tighten this set screw right here and there's a key already below it. I can see the key so we're doing good. This has been cut one too many times there.
We go okay, so tighten loosen each time. It'll go tighter, looking good! Okay, you want to make sure that this gap stays even when you're tightening it. That will make everything crooked that one's at one and three quarters they're about even right now. So we want to make sure we tighten them evenly.
That's good! Now, i don't think that's even anymore, that's right at two inches and that one's at two and an eight. So we need to loosen this one up just in here two and a sixteenth two inches. Actually, no that's two and two, that's even make sure we're still tight like it's supposed to be looks good not over tighten. I have got um all the contactors changed out and, of course, all the labels flipped back up indoor blower motors, installed, ready to be started up wired in aligned and everything, so we're ready to fire that up and check phase rotation and continue on okay, we're gon Na fire, this actually here's what we're gon na do. So i can be careful about it. We're gon na put the unit into test mode the shift unit test by doing that, it won't run when i power it on okay. Here we go and then now we can check rotation. So it looks like we have a call for fan and it's trying to start, but test mode is locking it out.
Okay, so i'm gon na go ahead and take it out of test mode. I'm gon na come on over here. It's going the wrong way. How did that happen? Oh, i know how it happened.
Yeah i'll have to uh reverse the rotation. I lined it up line one line two line three, but it must not be correct. Let's try this again: let's see if we're going in the right direction. Okay, we're going in the right direction! Now we just got to make sure that we're not over amping, so we're going to get in here and check current draw now all right yeah.
So, with the new motor we're allowed to pull 13.8 amps, so we need to go ahead and slow that thing down a little bit. We're gon na have to power this guy down open up the pulley all right. This motor is pulling too much current, meaning that it's running too fast, okay, so what we're going to do is we're going to adjust the motor pulley. So this is where i had it set right here was a half turn open, we're going to open it.
Two full turns to see if we can get it to drop so we're going to open the pulley. So that's one half there's one there's two, so we're gon na set it right there and then we're gon na see where that gets us all right. We're gon na see where this guy fires up at now so 13.8 is what we're allowed to run much better. I could even probably close it down a little bit, but i'm probably just going to leave it there so long as the building's air balance isn't jacked up and i'll check it on my way out, but we're going to leave it where it is.
I like to make it easy: i'm generally a lazy person so take this off, so i can access the motor right from the side instead of having to climb on top of the unit. I can do all the work from right here. All right. Everything is running.
Much better, i'm a happy camper, and now it's actually moving air before it seemed like it was running, really slow. Now we're really moving air, so all right we're doing good we're gon na watch. This thing operate for a little bit and start cleaning up. All of our messes man, where do you stop all of these relays, were burnt too look at these when you're out here in the desert and you've got equipment that is just not maintained as good as it should be.
You know i'm reluctant to not change those relays because, like i did because i don't want to be back, it's frustrating all right. Hopefully that's it on this guy check the td. It should be good, but look at these uh contacts, so they weren't horrendous, but they're. Definitely starting to burn and man - i don't know you guys, probably can't see it, but it is so smoky out here it's like starting i'm starting to get a stomachache. I don't know if it's the heat or the smoke um, but yeah every one of these contactors is like this. Just all pitted out beat down that's what the desert does to you. It's been about two weeks since the last footage and uh. When i finished up the motor install, i did not have, i had forgotten to bring up a limit switch to replace the limit switch that i had bypassed now mind you, we don't remember.
I just got to reiterate this. We don't bypass limit switches, especially on heaters. Okay, gas-fired appliances, or anything like that, anything where there could be a potential safety problems, never bypass high pressure controls any of that stuff. Now, when i bypass this limit switch, i literally did it just to get the unit operational and i turned off the gas so that way it could not fire up.
I have a new limit switch right here. We're gon na get this guy wired in. I have power, turned off and uh finish this job up, but yeah no complaints from the customer um. The ac has been working, fine blowers good.
So when putting these limit switches in um, they do this on purpose. There is a connector that is really tiny compared to the normal size, connectors. Okay, you got to make sure you have those. I keep these in my truck for this purpose.
It's so that way, you hook them up correctly. Another thing too, to clarify in the beginning of this video, i showed that i thought the uh, or i think i showed it at least when i, when the limit switch broke, all of a sudden um, the blower motor started running, and it was weird, like you Know something was funky there and it is a design of the unit that way. If the limit switch fails, they run the blower motor just to be sure that there's no potential of a fire in the unit. It would be in my imagination.
So when i push this guy in, i have it powered right now see the blower turned on, so they do that on purpose. For safety reasons, i would assume okay, i'm not the engineer that designed it, but that makes sense. In the case of this video, i bypassed a heater limit. Switch okay, you don't ever do that when you have an operating heater, okay or gas-fired appliance, never bypass a safety switch all right in this situation.
What i did was when i bypassed that safety. I disengaged. I completely disconnected the heating circuit, so it could not potentially come on. Okay, be very, very careful about that stuff.
This was one of those things where it was just. You know one thing after another and you know i'm so adamant about the wearing headphones when you're on the roof guys, i would not have heard the bearing going bad. It was an intermittent problem and i could not figure out why the breaker was tripping. The customer said they or actually the customer didn't even know that it was tripped but um. I couldn't find a reason and then i heard that sound and then it was like. Oh okay. Now i get a bunch of people asking me hey. Why don't i rebuild or replace the bearings in the motor? It's not economically feasible.
Basically, the amount of time it would take in labor would far exceed the price of the motor. So it's just as cheap to slap in a new motor but anyways we got the unit operational. The customers happy still never had another problem with that kitchen ac. I don't know what they were talking about that first time, but yeah all was well.
So i really appreciate you guys making it to the end of the video on this one. Do me a favor um remember i do uh live streams monday evening. 5 p.m: pacific on youtube, work permitting uh, also go live on the hvac overtime channel on friday evenings. With my buddies, we do just kind of a good hangout show and uh.
If you guys are interested in supporting the channel there's a couple different ways you guys can do so you certainly don't have to i'm going to keep making these videos support or not. But if you choose to do so, you can support me via patreon. There's links in the show notes of all my videos support me via youtube, channel memberships, merch available at hvacres.com. You guys can get shirts and hats um and then true tech tools.
Okay, if you guys are considering purchasing any tools, go to truetechtools.com use. My offer code, big picture one word and if you guys do know what tools you're looking for shoot me, an email i'll generate an affiliate link. It helps me out a bit more. Okay really really appreciate you guys and we will catch you on the next one: okay,.
In comparison with european standards a sloppy wiring system.
Easy to maintain.
I always love to watch various troubleshooting methods. There's so many skills that can overlap into other things, so any skills I can pick up are never a waste.
Thanks for putting the extra work in to show how it's done! Are you in Ottawa ?
I'd hate to say it, but honestly I love the vibes when a sequence of condensors turn on one after another. Good vibes. Are you in Barrhaven ?
What a mess inside units. Where was a Maintenance manager to keep it in clean conditions. Belts waiting to jump into fan. Just for Fun. But could damage a lot.
Got me on the wiping grease thing…I will do it from now on…Never realize I was such a hack
I miss my rooftop service….Carrier VAV is for me
Umbrella Hat/ Panama Jack Hat makes a world of difference 🙂
In the automotive would we use a short broom stick, long screw driver put it to your ear and the item. You will defiantly be able to tell if a bearing is going bad. Service area Nepean??
Just put a long screwdriver to the motor and the other end to your ear. You will hear it when the bearing is kaput!
The inside could have a leak. Run a line pressure test. If the condenser is empty, it will trip the breaker, but it's an inside unit issue or a leak at the ball valve.
No idea how I got here… but this was a pretty cool video. Service area Ottawa??
Great vid man, appreciate you taking the time to share. That invoice must have been nice! Keep up the great work!
I knew these units were complex, but never like this. New found respect for HVAC.
I really appreciate your videos and this one was particularly informative and interesting — particularly the detail you provided on resetting and tightening the pulleys. Thank you!
I'm guessing compressor grounded or contactor Are you in Nepean ?
20min and $30 worth of bearings is just as cheap?
Sir, you are amazing, very very professional, love whatch you videos, thanks.
🌟Please if you can buddy, could you record your new component replacements? . Like motors/ capacitors and relays/. Ext: That would be so cool ! 👍🏻👍🏻👍🏻👍🏻👍🏻
Loving the relays clicking one by one. So AWESOME 😎👍🏻
Loving this video mate. Love AIRCON UNITS.
VERY INTERESTING VIDEO. KEEP EM COMING
thanks for sharing 👍🏻😉
👍🏻👍🏻👍🏻👍🏻👍🏻THUMBS UP👍🏻👍🏻👍🏻👍🏻👍🏻
Anthony, derby, United Kingdom
A mechanics stethoscope will help find bad bearings.
I wish we had 30% humidity in the summer we always have 100-% humidity here in southeast Oklahoma
Well damn I wish all heat and air guys were this honest detailed and just damn right good!!!!
We use mobil EM grease on all our motors and pulleys/sheaves and it holds up really well in our DHUs that run about 0.1% humidity
Can these motors be refurbished? Seems not a difficult to replace some bearings. Clean insideout and lubricate. Good as new.
I'm in Scottsdale Az nd I know your struggle with the heat n humidity bro nd yes they whoop your ass good 🥵
I like your attention to detail. As far as the California humidity goes, I'd be glad to send some from the East Coast!
How to get a lawsuit in 3 easy steps:
1: Bypass limit switch
2: Bypass safety interlock
3: Keep heat enabled
But in all seriousness, if you bypass a limit switch, for the love of all that is R-404-A, disengage the heat.
You should’ve just went ahead and put some grease zerts on the motor
Hi sorry I don’t know your name but i am new to your channel
But could the kitchen AC be helped by the restaurant AC once you had it back up and running due to the kitchen extract if you are using the AC for the positive building pressure
Why is it that the blower motor lower amps by moving the pulley?
Were the hood exhaust fans working in the kitchen. I had that issue. All RtU Were working great but the hood exhaust fans belt was busted raising the temp to 89
With such low humidity wouldn't evaporative coolers be a much more efficient cooling option or is there just not enough water in Cali for that? I live in the Southeast and it is way more humid here.
I certify these units 🤩🤩😘 INTERTEK listed baby!!!
There are people that rebuild motors. Growing up, that's what I did a lot. Are you in Kanata ?
Nice job cautioning about bypassing limit switches.
This guy is awesome ive learn so much in one week watching his videos . hia communication is impeccable Service area Orleans??
Would a good IR thermometer have been handy in determining exactly which fan component was having difficulty?
Was that blower amperage draw enough to isolate the problem at the motor even while listening to Megadeth?
30/40% don’t even come to Georgia we’ll show you humidity
How much of a riot is that they told him it was the kitchen a/c?
Respect for being able to work in those temperatures!!!!!!! Man .. i am wrecked at 30 degrees celcius already …..